Needless to say to get the broken bolt out the whole front of the engine had to come off. So not letting a good crisis go to waste I decided since I was going to have it torn down I might as well upgrade while I was in there, so the old sloppy timing chain had to come off and I decided to upgrade it with a gear drive, because why build shit, when you can overbuild shit! The cast iron water pump got replaced with a new heavy duty aluminum unit.
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I went ahead and swapped a rebuilt Motorcraft 2bbl carb while I was at it.
Today's project was a cosmetic upgrade for the broken old steering wheel on the '75 Econoline.